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The New Secret Project !
Mr Ed gets more valves...
Edwards MR2 engine transplant.
Task... Stick together a slightly more esoteric 16V Mini than
the common as muck Honda/Vauxhall conversions...
Measured up the engine in Elaine's MR2, just to see if a 2.0
3SGE would fit, but the dimensions all looked a bit keen as the engine is fairly
tall and depth of the gearbox and diff seemed a bit tight too, shame coz they do
rev nicely !
No - I didn't pull Elanie's engine out for this - it's a pic I
found on the interweb! (Of the wrong engine - but you get the idea).

But as a consolation, the 1.6 4AGE engine from the MK1 is a bit
smaller, pokes out a respectable 120 bhp, redlines at 7700rpm and has a convenient
shape inlet manifold.

7th June
Bought two MK1 MR2 (4AGE) engines & 1
gearbox for the silly sum of £100, the day before another 4AGE without box had
sold for £180!!! Don't you just love finding things that have been incorrectly
listed so no one else finds them ;-)
Engine1 and box will stay together for the first fit, while
engine2 is being stripped for a rebuild - note the Spagweld engine stand!

Ed's engine bay and the thing that has to go in.

And a quick bit of photoshoppery to join them together!

Engine1 turns over by hand with no scary crunchy noises, and has
a nice firm bouncy compression.
Engine2 turns over just as smoothly, which was a bit of a
surprise as it has no plugs and there is a hint of water in one of the cyls. The
seller said that the engines had just been outside for about a month, but you
never know, do you ?
Pulled the head of Engine2 and found a little soft sludge, but
no rust or other scary things, so may be OK!
First job is a bit of a clean with some handy shed chemicals...

Must remember to rinse the bits before they all fizz away...
9th June
Head has come up pretty well without disolving, and the valves
all look pretty good

Slight modification to my valve spring compressor coz the Yamaha
developed head uses teeny caps & collets to hold the valves in. (Rumour has
it that shims for their motorcycle heads are the can be used coz they are the
same size...)

Big inlet ports for the variable inlet thingumies.
Inlet manifold and the variable inlet thingumies being de-cacked.

Bought an interesting Honda frame that seems to be loosely modelled
on the GoMini one, £400 is a big enough chunk, but will save 3 or 4 days of
modding a std subframe, or building one from scratch. Not very pretty, but
should do the job :-)

Ha ha, how sooper is that !
My gamble seems to have paid off, and after 10 mins with the hacksaw to remove
one of the Honda mounts, the MR2 lump just slipped in OK.

OK, the alternator bracket needs to come off so that the engine
can sit further back, then I need to weld up some mounts for the MR2 lump, but
all looks promising!

14th June
Decided to use Ford EDIS for ignition so that I can get rid of
the dizzy, which may make a bit of room for the alternator to sit on the 'wrong'
side of the engine.
Modified the Pievan's Megasquirt as this one is now going in Ed
(poor Pievan!)
A couple of links and some component swapping should mean it's
EDIS ready.

16th June
EDIS stuff arrived, and it's rather magic really, plug the
module and coil pack together, then 4 wires to make it work. So simple an 8yr
old could do it - if they could tear themselves away from the Playstation to dig
out the Lego ;-)
Simple test rig to check it all works...

Um, some sparks, meaning that it worked fine !

17th June
Picked up another Ebay gem, a MR2 gearbox for £10, admittedly
I paid another £20 for the driveshafts, but not a bad haul fer £30 !
In the afternoon, welded the trigger wheel onto the pulley and
welded up a bracket for the sensor.
18th June
Loom time, stuffed the coil pack in a handy space above the
gearbox and started making up the engine loom....

By knitting the cables around various things in the shed.

Leaving a few offcuts !

Then invented a '20 minute' manifold recipe.
Take a stock cast manifold, chop a couple of bits of steel pipe
and weld on, squishing the ends to fit the next bit o pipe.

Attach the next bit o pipe and leave to cool for 10 mins :-)

Well, obviously with the 'lectronics in place and a bit of zorst,
it would only take a bit of fuel and the engine should fire up, right ?

Engine Test #012.5mb avi
(DivX5)
24th June
Made quick bodge blanking plate for the distributor out of some
8mm thick aluminium.

With the help of Neil, we pulled out the 1380 removed the Mini subframe and stripped off
the suspension components.
Chopped the front panel and inner wings, then trial fitted the
new subframe.

Found that some of the suspension pick up point's were not quite
right, so decided that the easiest (quickest) way to fix it would be to glue the
back of the standard Mini subframe to the front of the new one.
Also... Dropped a trolley jack on my foot :-( Luckily it
wasn't the big jack !!

25th June
Spent a couple of hours on the spare head... Exhaust valves
cleaned, lapped in and refitted. Then for good measure stuck the zorst cam in
and lobbed the cover on. Zzzzz boring job, will leave the inlet for another day
;-)
Mr Neil popped over again to assist and generally offer
sarcastic comments about my craftsmanship...
Chopped up the Mini frame and fitted the remains back on the
car.

Then chopped the new frame and welded them together to make some sort of
b45tard hybrid offspring.

Dangled the engine into the hole and kept trimming
around the edges until it fitted in.

All looking good, but the inlet manifold is fouling slightly on
the bulkhead by the master cylinders, so this will need attention to make a bit more room.

26th June
Tried to get adjuster rides to turn & separate from the rubber
breasts, all seized up, so coilovers it is then ;-)
Had a brain wave... If I take out the TVIS butterfly plate, then
the inlet manifold suddenly gets 20mm shorter, which should help with the
clearance and it's one thing less to have to control ;-) I don't think the Mini
is heavy enough to have too much of a problem with loosing a little bottom end
torque or economy !
Out with the TVIS,

More room!

Pulled the engine back out, trimmed bulkhead x-member and master cylinder drip catcher and
welded in a recess for the inlet.

Also trimmed bits of subframe to
clear the diff.
27th June
Rebuilt the inlet valves/cams on the spare head, so that's all
done and ready now.
Went a bit MIG crazy and seam welded a load of joins & cut
edges on the subframe, then spent a couple of hours tweaking the coilover
brackets and assembling them with some nice GAZ rod ended shocks. Handily I had
a spare pair of 250lbs springs from Pievan testing, which should be about right.

Dropped the engine back in and roughly located it with some top
quality 'bit-o-wood' mountings. Much better clearance to the bulkhead and scope
to mount it higher to improve ground clearance.
28th June
Spent most of the day making the final engine mountings -
a time consuming job, but probably quite important to get it about right!
Engine needs to be centred so the front wheels don't foul the
crank pulley or gearbox, needs to be nice and straight across the car, needs to
be mostly horizontal and there needs to be the minimal gap between the back of
the engine and bulkhead (less than 10mm). Oh, and lastly the mounts need to be
easy to reach, easy to use and must take up as little engine bay as possible.

Results are good, the engine is nice and solid with as much
space as possible left for the radiator and other junk :-)

Chopped the front off the bottom arm pins, fitted new bushes and
welded some locating strips hold the front ends in place. Suspension is now
finished and just needs the angles checking.

29th June
Another time consuming job, this time the gear linkage. This one
needed a bit of thought to ensure that the gear stick ended up working the right
way after reversing it. Other things to consider:- fixed cable length,
routing of the cables, location of shifter, leverage ratios - and a small,
simple design (right, no pressure then!!).
After much head scratching this is revision #1. The cables run
tight to the box to save space, and are connected to give the smallest shifter
movement possible, which should result in reasonable travel when the stick gets
lengthened. (The extra spiky bits will be lopped off when it's all been tested
properly!

The MR2 shifter thingy fits nicely to the floor unlike the huge
comedy beige plastic lump you get with the Vauxhalls ;-) The stick will need to
be extended for a comfortable reach.

Then onto making the final exhaust - 2" bore with 2 boxes,
hopefully should have reasonably deep note, but not be too loud and chavtastic
;-)
Extra wiggle welded onto the fanny-mould to get the pipe in the
centre of the tunnel.

Jetex rear silencer with the old RC40 tail pipe welded on.

Jetex intermediate box.

30th June
Chopped up the removed bits of front panel then welded the
corners back in place on the car, the middle bit behind the number plate
comes off with the bumper for easy access .
Trial fit of the Corsa radiator looks reasonable, although it
took a fair bit of juggling and fettling to get it to squeeze in with the fan !

Extended the gear stick, modified the Mini gaiter to fit, then
lobbed the carpet back in. - Also got Elaine to be an ergonome and er, test the
ergonomics :-)

Removed the inlet manifold, drilled an 18mm hole in Y piece,
then welded a 1/2 nut in place to make a boss for the O2 sensor.
1st July
Spent the morning creating a bracket for the alternator, to
squeeze it in under the headlamp, then measured the belt and tootled off to
Halfwits. Found the nearest belt size was 10mm longer so redesigned the bracket
- poop !

Fitted the sooper-Spag relay / fuse box to the bulkhead, and
mounted the EDIS module underneath, then installed then engine loom, which, due
to a slight change of plan needed a bit of editing.

Here's a shot of the EDIS VR sensor and 36-1 trigger wheel -
this time not a LEGO install ;-)

2nd July
Sunday, so had a lie in and didn't venture outside until 0630
:-)
Spent a couple of hours playing with wiring and other 'lectrical
stuff, then Neil came over and got horribly frustrated in the blazing sun,
trying to wire the front lights back up. He had a damned good excuse though -
some of the 1975 BL wiring had changed colour due to age & oil
contamination, turning blues into greens !!!
I also had a fun job trying to diagnose why we were not getting
any sparks until Neil asked if the timing strobe actually worked. Sticking a
screwdriver up the plug lead showed that the strobe had died. Poop more wasted
time :-(
But after these little technical hitches were overcome, we
quickly plumbed in the cooling system.

Then added a temporary fuel supply and fired the engine into
life :-)
Very pleased, using a mostly default map the engine sounds
pretty sweet with 60+psi of oil pressure at 1300rpm, then after a bit of
fiddling got a nice stable 600rpm idle too !
05_run2.avi - 7670kb
DivX avi of engine running in car.
Then unwound in the cool of the evening by fiddling about with
the removey front panel thing.

Which fits in the 'ole with 4 bolts.

Then the grill screws in.

Doesn't compare too badly with my earlier fake pic ;-)

In all, quite a discrete install !

Still got a few things to do before driving though....
Driveshafts, fuel tank, brakes, and a bit of dash wiring etc...
I think I deserved the big celebratory beer !! (Hope Neil had
one too!)

5th July
Modified a standard 7.5 gallon Mini tank for fool injection by
welding a 'Spag-sump' fuel take off to the bottom...
A suitable steel can with a pipe fitting welded on forms the
sump that will collect fuel from the bottom of the tank. It's not very big, but
will hopefully stop the pump from sucking air on acceleration or cornering -
when the tank is running low...

The sump fits on the bottom of the tank and the fuel drops
through these holes...

NOTE - welding something that has contained petrol can be a bit
risky and potentially fatal, so... don't do it !
This tank has not been used for 7 years and has been left
uncapped for that time, bit it still had a petroly smell ! So, to make sure the
tank wasn't going to explode while welding I chose the super safe option of
remotely applying a match or two.

After a distinct lack of detonation or even feeble fire I
proceeded to the next stage in preparation of welding.
During welding the tank had (recycled) water running through it
and an extinguisher on standby.

The Spag-sump welded on with no incidents and to make sure it's
leak proof a thin skim of chemical metal was added.
Tank still fits :-)

So after a quick lick of Hammerite the fuel system is now
working (if not fully bolted in...)

8th/9th July
Mr Neil assists again :-)
Removed the radiator to make space for the new front brake
plumbing and Neil lobbed on the flexi hoses, then he went off to the back of the
car to fight with fitting the rear flexies and some smaller bore cylinders.
New radiator/fan brackety frame thing for a more solid mounting
than cable ties !

A nice collection of copper plumbing fittings, chopped up hoses
and cable ties plumbs in the heater and bypass pipes.

After running the engine up to temperature and flushing the poop
out we spotted that the water in the swirl pot was flowing the wrong way :-(
Turns out that the Toyota engine has the stat the other way
round... So instead of the stat opening to let hot water out to the radiator, it
opens to let the cool water in - bugger!
With a bit more plumbing, it all works the right way round now
:-)

Next tasks were 'lectrics and shafts, so Neil sets about cursing
the 20years of sundry mods and bodges to the loom, while I get busy with the
MIG'n'grinder.
Washers, new indicator switchery, accessory socket & 'orn
all working.
Mini & MR2 drives hafts measured, re measured, measured
again then chopped up and welded together again, results were remarkably
straight!
The nearside shaft is pretty short, so the CV boots will almost
overlap !!

Offside shaft in position. (Don't worry, there really is plenty
of space between the brake hose and choppy EDIS wheel !)

Last job:- tighten/ grease suspension & check the wheel
nuts, then test drive :-)
Ok, so due to a wiggly -ve connection the Megasquirt wouldn't
fire up, but after that extra last job was sorted it was test drive time.
***
ED MOVES !!! ***
10_ed_moves_1.avi
Neil gets the first drive 9112kb DivX avi
OK, so the front grill rattles, the throttle return spring is
too weak and the fuelling isn't mapped - but it works!
Um, yup, it definitely works :-)
Felt a bit grindy under acceleration, so the box may be a bit
crappy - or maybe just needs the oil checking !
Pesky alternator seems to be stuffed, so that will need sorting
before any real on road tuning, but doesn't seem to major.
Good progress though (ta again Neil) so time for a relaxing pint

23rd Sept
Speedo update...
Due to a bizarre twist of fate it turned out that the speedo in
Ed just happened to be accurate to within a couple of MPH when connected to the
MR2 gearbox :-)
However, modifying the cable to work reliably was a bit more
troublesome, but after several failed revisions it was time to get serious! I had tried epxoying the Mini square plastic end bit to the MR2
cable but it failed a couple of times, so the MIG came out and I welded a blob
to the end, then filed it to shape.

A bit of thin steel tube crimped over the end of the outer cable

And a larger bit epoxied to the end fitting thing cut from the
original Mini cable.

Then the whole lot just clamps together, and the length can be
fine tuned for the perfect fit.

3rd Nov
Rolling road.....
Well, considering Mr Toyota claimed the engine should stick out
about 125bhp (when new in 1986), we were quite pleased to find that our £50
bargain Ebay engine was putting out nearly 130 at the wheels :-)
Hooray for us, Elaine's Megasquirt tooning skills and the spagbodged 'freeflow'
exhaust system!!
Actually, removing the TVIS butterfly plates has probably
improved the top end a bit at the expense of a little bottom end torque.
But having said that it still has twice the torque of an A
series, so there's more than enough to go round...
Peak torque 148 lbs ft @ 4000 rpm
| RPM |
BHP (flywheel) |
| 3000 |
77 |
| 4000 |
108 |
| 5000 |
132 |
| 6000 |
138 |
| 6500 |
135 |
A few vids, squished with DivX
Edited highlights.
ed01-dial1.avi 1.2mb
ed03-short.avi 4.4mb
And here's the longer one (yawn)
ed02-med.avi 18.2mb
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